Kathmandu,
Jan. 27: The US Bangla Airlines that crashed at the Tribhuvan International
Airport (TIA) on 12 March 2018 had met with the accident due to disorientation
and complete loss of situational awareness by crew members, concluded the
Aircraft Accident Investigation Commission (AAIC).
“Contributing to this, the aircraft was offset to the proper approach
path that led to maneuvers in a very dangerous and unsafe attitude to align
with the runway,” concluded the AAIC led by Yajna Prasad Gautam, former
government secretary.
It submitted the report to the government on Sunday.
According to the report, there was clear evidence that the pilot was
harboring severe mental stress. He was irritable, tensed, moody and aggressive
at times. He exhibited undue aggressive behaviour and anger at the ATC
personnel as well as operation staff.
The pilot had also used foul language and abusive words in conversation
with a junior female first officer. He seemed very unsecure about his future as
he had submitted resignation from the company verbally. He said he did not have
any job and did not know what he was going to do for living, read the report.
The
Cockpit Voice Recorder (CVR) and passengers confirmed that the pilot was
smoking in the cockpit.
The report said that landing of the aircraft was completed in a sheer
desperation after sighting the runway, at a very close proximity and very low
attitude. Similarly, the pilot did not attempt to carry out go-around when a
go-around seemed possible until the last instant before the touchdown on the
runway.
The loss of situational awareness forced the pilot to make some
dangerous moves of aircraft at a very low altitude in the hilly and mountainous
terrain around TIA.
After impact on the ground the uncontrolled aircraft ran out of the runway, hit the runwayperimeter
fence and rolled down the slope into the grass field and caught fire which engulfed
theaircraft, read the report.
“It is evident that there were a number of procedural violations during
the flight by the cockpit crew,” read the report. “The pilot seemed to be under
stress due to behaviour of a particular female colleague in the company and
lack of sleep the preceding night.”
The
investigation committee also concluded that the pre-flight briefing and
commencement of flight departure was made at improper timing – operational
pre-flight briefing was given early morning but the flight departure time was
around noon and there were four domestic short flights scheduled in between.
The
aircraft was performing its scheduled flight from Dhaka, Bangladesh to
Kathmandu.
According
to the report, there was no evidence of any defect or malfunction in the
aircraft that could have contributedto the accident. There was no evidence of
system malfunction prior to the accident.
“ATC at the
TIA tried their best to assist the pilot providing landing opportunity at any runway
in convenience of the pilot and ensuring the airspace clear to avoid further
conflict with other aircrafts.”
The
accident killed 51 passengers including 4 crew members – 28 Bangladeshis, 22
Nepali and 1 Chinese, and injured 20. The aircraft was completely destroyed in
the accident.
Published in The Rising Nepal daily on 28 January 2019.
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